LX200 Mods


Here are a couple of miscellaneous things I've done to my LX200 to make it more usable.

I added a counterweight in the fork arm opposite the dec drive. With the various weights I am using it is possible to get balance good enough to be able to release the locks and leave the OTA pointed in almost any orientation without it turning. The other weight in the photo is about 7lbs used to balance the guide scope. First balance the scope about the dec axis then about the RA. If you break this down into to seperate tasks it's MUCH easier.

This is my power distribution box, basically a home made 12v outlet strip. Each plug leads to a heater. The two free outlets power the window heater on the camera and my light box.

Adding a sheet of Teflon under the wedge make adjusting the azimuth during alignment much smoother. (see next)

I made an azimuth adjuster out of a turnbuckle from the hardware store, a left and right hand threaded pair of bolts and some 'L' brackets, Teflon washers, nylon filled lock nuts, and a Pepsi. The knob is the lid from a medicine bottle that I cut a hole in, slid over the turnbuckle and then filled with epoxy. One end is anchored to the 'BB2200 scope saver plate' under the wedge and the other is attached to the wedge. The hexagonal cross section of the turnbuckle is useful. When drift aligning I've learned to think in terms of a 'full flat' or 'half flat' of adjustment.

Looking down on the azimuth adjuster note the label indicating which way the knob rotation will move the north end of the polar axis. This is so much better than the absurd system Meade supplies that requires you to adjust two knobs at once with your arms wrapped around the scope all while standing on the wrong side of the scope for what you are doing.

Since I roll my scope out of the garage to observe I use a set of 'JMI Wheely bars'. As supplied the ends of the cross members can be twisted which means the entire scope can wiggle slightly in azimuth. I use reference marks painted on the driveway to avoid drastic realignment. I wanted a more rigid structure. I made a large 3/4" plywood gusset that adds weight to the assembly and prevents the cross members from twisting.

I replaced the supplied adjusters with plastic hand knobs with pieces of 1/2" all thread rod with a nut, lock washer, fender washer, lock washer, nut assembly on the end. This allows me to use an automotive breaker bar with a 3/4" socket on the end to adjust the tripod from a standing position where I can keep my eye on the bubble level.

This shows one of the adjusters with the 'leveling tool' slipped over it. This method is 5000 times easier than squatting to turn the knobs and then 'prairie dogging' up and down to see the level.

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